Jump to content
SAU Community

Recommended Posts

Hi, I need help changing my stock air intake to pod. I was in the middle of removing the stock air box. Iv unbolted everything but can't seem to remove the maf from the hose. Iv undone the jubilee clip but it's not budging. Pic has been attached and I will resume once the rain has stopped. Any help is appreciated! 

20191109_145005.jpg

Link to comment
https://www.sau.com.au/forums/topic/479136-help-installing-pod-filter/
Share on other sites

38 minutes ago, Murray_Calavera said:

You say you've unbolted everything but in the picture there are still many bolts?

Go forth and remove bolts, this should be a very simple job. 

Do I need to remove the 4 gold bolts circled in red? Everything else is unbolted and iv been trying to remove it via from the hose circled in green if I can free it from there then the whole box and maf will come out. Thanks for the help 

20191109_180507.jpg

They're holding the AFM to the airbox. Seeing as you've loosened the hose clamp, if you want to slip the AFM off the inlet pipe, to make it easier to work on the AFM to airbox on the bench/lap/whatever, then just pulling the AFM out of the hose would be a good start.

2 hours ago, GTSBoy said:

They're holding the AFM to the airbox. Seeing as you've loosened the hose clamp, if you want to slip the AFM off the inlet pipe, to make it easier to work on the AFM to airbox on the bench/lap/whatever, then just pulling the AFM out of the hose would be a good start.

Will I have to remove those 4 bolts anyway to connect that side to the hks air intake? 

Just remove the bolts. Sounds like you reallly want to!

Yes you will have to remove them to attach the pod, that should be fairly obvious.

then sit back and enjoy the pointless mod you have just implemented.

You seem to be scared of undoing those 4 bolts.

You also seem to have hit a road block.

My advice would be, remove the bolts. You might find it helps. If it doesn't, you'll be surprised that you can do them back up. 

Don't be scared to have a go and try things. If your paranoid, take lots of photos and put the parts/bolts into resealable plastic bags and label them.

On 10/11/2019 at 8:07 AM, Murray_Calavera said:

You seem to be scared of undoing those 4 bolts.

You also seem to have hit a road block.

My advice would be, remove the bolts. You might find it helps. If it doesn't, you'll be surprised that you can do them back up. 

Don't be scared to have a go and try things. If your paranoid, take lots of photos and put the parts/bolts into resealable plastic bags and label them.

 

Thanks everyone for the advice. I couldn't get to 2 of the bolts as those gold bolts can only be removed from the opposite side. I was scared of applying too much pressure on the hose and tearing it so in the end I decided to get 2 big flat head screw drivers and pry away and it came off easy. After that it was all good and its now on the car. The car sounds amazing can hear the turbo spool up loud like a jet. ???

Edited by 020king
1 hour ago, niZmO_Man said:

Shame it's making less power now.

But it sounds like a jet..

OP, put on cover, it will still sound whoosshhhy, but be more legsl and less hot air

 

Create an account or sign in to comment

You need to be a member in order to leave a comment

Create an account

Sign up for a new account in our community. It's easy!

Register a new account

Sign in

Already have an account? Sign in here.

Sign In Now


  • Similar Content

  • Latest Posts

    • Power steering is probably because someone has nuked the HICAS CU and you no longer have the variable power asist doing what it is supposed to. How much boost are you running? You are aware that any more than 10 psi on the stock ECU is just asking for it to go to full R&R (that's Rich & Retard, which is effectively Retarded and Retarded!) which kills all the power. Depending on the exact conditions, it can just be runnign on the fat and stupid end of the maps, then the conditions change, you make a little more boost and the ECU goes into panic.
    • @BuiltNotBought Just as GTSboy said.   If you want driveabilty and more low down torque..keep the stock runners. They are VERY good from a factory. I have them too on my RB25DET NEO and as a GTSboy i have fmic but with stock piping route(i have Blitz intercooler) Iam making around 320 BHP and the car pulls "hard" from like 2,5k all the way to 7k. I have it dyno tuned to mimic N/A power curve and making little less max torque due to the smallbox tranny. But driveability is very great. I had 350Nm below 3k so car feels very quick.   EDIT:  Not my channel but i saw this and i know that is what i want (and i have exactly this)  
    • Looking to sort out a couple of issues on my skyline  It recently was rebuilt, however rebuilder long story short did not give two flying effs about the work he did. So moving forward it's running but I have two persistent issues 1) it has a misfire / lag type of issue (was at higher RPMs but I had a dead piggy back ecu removed which improved it) now it's not as bad but still does it at random, I thought it may have been a boost issue I'm running an older turbosmart dual stage controller, turbosmart told me to try running off gate pressure however it still has a lag at random times. It has New MAF, maf plug, coil packs, sparks, CP harness.. injectors tested and cleaned. Factory ECU. 2) Power steering issue. It is tight as anything. Flushed power steering, rebuilt my pump because the bearing was shot. Flushed again still tight (mainly when parking and going slow into my driveway etc)  No kinks in hard lines, replaced the lines I could see had cracks. Still tough to steer.  I was told to shim a coin and place into the solenoid plug? Is there anything else. My steering angle sensor also has a issue. It's a used one I replaced, does it need to be calibrated? I feel like I've tried everything and this car is my voodoo doll.   
    • Holy shit... wow!!! I totally missed this
    • One main filter. Each tank has a prefilter to keep rocks and small children out, then the big main filter that also does water separation. Clogged the first one so bad it was like a rev limiter at 3200rpm. Literally just like dropping the throttle off and maintaining rpm!
×
×
  • Create New...